eltham well hall train crash

Latest Documents Further Reading The 20:05 return excursion train crewed by Wilsdon, Stokes and Atterbury consisted of a British Rail Class 47 locomotive, No.1630 from the Midland Region, and ten coaches; a Brake Second Corridor, a Second Corridor, a Composite Corridor, three more Second Corridors, another Composite, a Tourist Standard Open, another Second Corridor and another Brake Second Corridor at the rear. News Stories As well as Wilsdon, two passengers died at the scene; a woman later died of her injuries in August and a male likewise in November, bringing the number of fatalities to five. Although it was agreed that the signalling played no part in the collision, it was later agreed that the signals around Eltham Well Hall would be redesigned to slow a train to round the curve rather than remain at green, which would mean it would be less likely a driver would be caught by surprise with the curve. Pin on Eltham and Environs - Pinterest A concrete-lined cutting accommodating a dual-carriageway was envisaged, this of which would run parallel with the Bexleyheath Line for about a mile in the vicinity of Eltham, before passing under the railway at Well Hall. British Rail staff who came in contact with Wilsdon on 11 June (his supervisor at Hither Green, depot staff at Ramsgate, Secondman Stokes, Railway Club staff at Ramsgate, Guard Atterbury, Stationmaster Arundell and his staff at Margate, Railman Fleming and Signalman Obee at Rainham) were all intensively questioned and gave evidence at the inquiry regarding the state of Wilsdon, to which all agreed that Wilsdon appeared perfectly fit and sober even as late as his unscheduled stop in Rainham, with the only person aware of Wilsdon already having drunk alcohol prior to reaching Ramsgate being Secondman Stokes, who considered him still fit and sober enough to drive the train. Approaching Eltham Park he became so concerned at the speed that he made two quick applications of the vacuum brake to try to draw the driver's attention, but before he could get a reaction it was too late. The rear of the coach had been somewhat damaged by the fifth, sixth and seventh coaches passing by it, derailed but still on the track. Notable survivors of the 1931 rebuilding at all three stations mentioned were the SER timber waiting shelters. Book: Ministry of Transport . According to his notes, the train passed through Bexleyheath at 21:31, seven minutes behind schedule (estimates showed that Wilsdon had made up at least a minute and a half between Gillingham and Strood) and was running on clear signals. GitHub export from English Wikipedia. 1630 (latterly Class 47 No. Robertson . The locomotive jumped the sharp curve, derailing and rolling onto its left side and sliding through a coal yard. The secondman may not have been attentive because he had also been drinking, but he did not know the route and would not have realised that the driver was not braking for the curve when he should have been. This document was published on 1st June 1973 by Department of the Environment. According to his notes, the train passed through Bexleyheath at 21:31, seven minutes behind schedule (estimates showed that Wilsdon had made up at least a minute and a half between Gillingham and Strood) and was running on clear signals.[2]. The guard told the inquiry that after leaving Rainham he had noticed that the train's speed has been "a little bit excessive" and that the driver braked intensely between Gillingham and Chatham. Arundell believed that they were a gift left by the organisers of the excursion to the engine crew - such being a normal 'tip' for excursion drivers to enjoy off-duty - and he did not question their appearance. D1677. The driver Robert Wilsdon and five passengers were killed, and 126 people were injured. The inquiry hypothesized that the driver had taken spirits into the cab with him, having collected them during his unexplained absence before leaving Margate. Both Wilsdon and his colleague were reinstated on 18 December 1961, with Wilsdon being promoted to driver less than a week later on 25 December with his transfer to Hither Green. United Kingdom. He stated that he was thoroughly ashamed and that he had been celebrating a promotion to the position of Passed Fireman with his colleague who greatly assisted him. Investigating this theory, the morning after the accident, the cab was searched and three smashed glasses were found in the cab's wreckage. Places time Forgot London Bus East London London Areas Old Well Hall Bus Station 1970's J Michele Janes Eltham History Exactly where the pair went in this period is unknown owing to Wilsdon's death and Stokes having little recollection of the events after leaving Ramsgate and although another pub was close to the station, it was considered that neither had time to reach it.[2]. Running slightly late and at Wilsdon's urging, the pair returned to Ramsgate Depot at around 19:40. Today. good people helping eachother, Ilford rail crash, Ealing rail crash, Wembley Central rail crash, Cannon Street station rai, Spa Road Junction rail crash. His speech was clear and his gait was normal. This took the platforms beyond the bridge which carried the running lines over Well Hall Road, and a new entrance was opened between the latter and the stations down platform, by means of a staircase upon the embankment. Well Hall - Wikipedia The second incident occurred on 28 March 1969, when Wilsdon was fined 1 for being drunk in Lewisham. These trains would be driven by Southern Region drivers for some of the journey (particularly to ensure that experienced drivers took the trains through the complex arrangements around Clapham Junction) and would, on reaching Margate and being cleared of passengers, take them onward to Ramsgate Depot where they would be stored until the return trip. A ten-coach excursion train, the 20.05 Margate to Kentish Town, hauled by Brush Type 4 No. Photograph by Press Association, 1972. A member of staff on the platform at this time noted that he had seen both Stokes and Wilsdon depart the locomotive and leave the station via Platform No.1 three minutes after having arrived at Margate and this was later compared with the timings made by Guard Atterbury, who recorded a 20:13 departure from Margate (eight minutes late) noting that both Stokes and Wilsdon were absent. Accident Root Causes Identification Using a Taxonomy - Academia.edu The empty train left Ramsgate and made an uneventful journey to Margate, arriving at around 19:59. Eltham Well Hall rail crash Wiki - everipedia.org Stationmaster Arundell signalled the train clear to depart for London, but both he and Atterbury found that there was no response in the cab. [1] It seems these splashes were too late and light to register in the cab. This was a very unusual action, particularly as he had made up almost seven minutes of the lost time. After the crossing was cleared, he set the route for the train to proceed but instead, the train came to a stop at the platform. The locomotive and first four coaches left the rails and came to rest at an angle to the track, the second and third coaches on their sides. When Stokes boarded the engine, he waited alone in the cab until around 18:25 when Wilsdon arrived and spoke about the preparations for the journey back to London. Contributions Eltham Well Hall - Kent Rail All three of these coaches were leaning over on their left sides to various degrees, with the leading end of the fifth coach having been badly damaged by the impact with the fourth coach. Robertson, concluded that the driver Robert Wilsdon had "grossly impaired his ability to drive safely by drinking a considerable quantity of alcohol both before and after booking on duty, including some shortly before leaving Margate and some more in his cab during the journey.". Eltham Well Hall. Owing to the large number of day-trippers booked for this customary annual works-outing, a pair of excursion trains were laid on to transport them to Margate and back. The recommendation that booking-on by telephone be carefully controlled was reiterated in the Inspectorate report of the Cannon Street Station rail crash in 1991. http://www.railwaysarchive.co.uk/eventsummary.php?eventID=134, Images of the accident (approximately halfway down the page), https://infogalactic.com/w/index.php?title=Eltham_Well_Hall_rail_crash&oldid=202875, Creative Commons Attribution-ShareAlike License. However, this evidence was contradicted by a later statement made by Secondman Stokes that when they met at Ramsgate, Wilsdon told Stokes that he had "ended up going somewhere and drinking some sherry". The second uncertain moment was what occurred to both him and Stokes during the stop at Margate, in which both seemingly left the station via the Platform No.1 entrance. There was an imbalance with the urine alcohol level which made it very likely that the driver had also been drinking alcohol within an hour of his death, meaning it was possible he had been drinking at the controls. Please consider donating to help with our running costs. All witnesses who saw the driver including the guard, the station staff at both Rainham and Margate, and the depot staff at Ramsgate, observed no signs of intoxication. Most Wanted The second excursion train, scheduled to leave Margate at 20:05 was to be crewed by Driver Wilsdon, Secondman P.E. Press Association. The last station the train passed on its journey that Atterbury had to time was at Bexleyheath railway station 4.3 miles (6.9km) east of the accident site. This travel time and distance between Rainham and Hither Green played a key role in the accident that occurred.[2]. He had been working on the railways since 1958 and was experienced to drive the British Rail Class 47 locomotive, which would occasionally come down from trains in other regions. He briefed the pair on the train's particulars with Wilsdon appearing sober and routine. Upon completing his phone conversation, Wilsdon returned to his cab and departed having been stopped at Rainham for about four minutes. An excursion train from Margate to Kentish Town derailed on a sharp curve at Eltham Well Hall station, Eltham, London. In the cab, Stokes later recalled that Wilsdon had suddenly shouted in a frightened way at the sight of the curve approaching, to which Stokes immediately braced himself in the seconds that he had available. Here, Wilsdon drank two pints of light and bitter and a half pint of light ale which was confirmed by his brothers who'd drunk similarly. As a result the heavy locomotive entered the curve at some 65 mph and, distorting the track and sharpening the curve immediately ahead of its wheels, overturned to the left and dragged the train after it into almost total derailment. The public inquiry into the accident eleven years later agreed that this incident was a seemingly isolated occurrence and all had reason to believe Wilsdon; the Line Manager who reinstated the two was not criticised for this approach, although some criticism was given to the Management in 1961 for promoting Wilsdon so quickly after being reinstated. According to them, the three returned home and spent the afternoon indoors with the children until Robert was driven by one of his brothers to Rainham station at around 17:15. Touch device users, explore by touch . Eccles Rail Crash . In contrast, Stokes claimed that Wilsdon mentioned drinking some sherry when they met at Ramsgate. The 1969 incident also showed Wilsdon's disregard of what had occurred in 1961 but it was agreed that the manager at the time had been unwise in waiting two months to question Wilsdon, but had acted appropriately when he did. The Bexleyheath line became fully track-circuited at this time and, in the same year, a check rail was laid west from Well Hall station, along what was known as the Well Hall Curve. The only other theory was that Wilsdon had obtained a bottle of spirits at some point, stored it on his person and had drunk it at some point after leaving Margate, and later disposed of the glass by throwing it out the window of the locomotive, with the theory being that Wilsdon either obtained the bottle at some point whilst in Margate or had kept one on his person since he left Rainham for work. The front of the cab was torn open and debris thrown and 'ploughed' inside, killing Wilsdon and severely injuring Stokes. This travel time and distance between Rainham and Hither Green played a key role in the accident that occurred.[2]. injuries= 126The Eltham Well Hall rail crash was an accident on the British railway system that occurred on 11 June 1972 at approximately 21:35. Eltham Well Hall train crash; Statements. The 1969 incident also showed Wilsdon's disregard of what had occurred in 1961 but it was agreed that the manager at the time had been unwise in waiting two months to question Wilsdon, but had acted appropriately when he did. The locomotive and first four coaches left the rails and came to rest at an angle to the track, the second and third coaches on their sides. After the crossing was cleared, he set the route for the train to proceed but instead, the train came to a stop at the platform. At 19:45 they met with the guard and drove the train to Margate to receive the passengers. Stationmaster Arundell signalled the train clear to depart for London, but both he and Atterbury found that there was no response in the cab. In reality, Wilsdon did not leave for Rainham station until 17:15 and as such his move was solely to gain pay for an extra two hours for which he had not actually been on duty. This evidence contradicts that of Wilsdon's brothers who claimed that he had not drunk between 14:02 and 17:15. The fourth coach had ended up roughly 90 degrees to the track, leaning over on its left side. Both men were subsequently suspended shortly afterwards, against which Wilsdon immediately appealed, claiming that the event was an isolated incident. More significant was the opening of "Shooters Hill & Eltham Park" station, a mere 41-chains to the east of Well Hall. That day the Harrow Observer reported the horrific accident and 66 years later, getwestlondon pays tribute to the victims. Guard Atterbury was not criticised whatsoever for his behaviour and it was considered unfortunate that his "splashes" were too weak to gain Wilsdon's attention. [2], Coordinates: .mw-parser-output .geo-default,.mw-parser-output .geo-dms,.mw-parser-output .geo-dec{display:inline}.mw-parser-output .geo-nondefault,.mw-parser-output .geo-multi-punct{display:none}.mw-parser-output .longitude,.mw-parser-output .latitude{white-space:nowrap}512719N 00301E / 51.45536N 0.05019E / 51.45536; 0.05019, Events prior to Wilsdon arriving at Ramsgate, Learn how and when to remove this template message, Associated Society of Locomotive Engineers and Firemen, "Railway crash driver survived dismissal", "Accident at Eltham Well Hall on 11th June 1972", https://en.wikipedia.org/w/index.php?title=Eltham_Well_Hall_rail_crash&oldid=1142297435, This page was last edited on 1 March 2023, at 16:48. Its nameplates were salvaged, and transferred to No. Those who knew the driver said that he was quite a frequent drinker of alcohol and could "carry" much beer. Investigating this theory, the morning after the accident, the cab was searched and three smashed glasses were found in the cab's wreckage. He made recommendations that booking-on of drivers by telephone should be controlled carefully, but did not recommend any changes to warnings of permanent speed restrictions.

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eltham well hall train crash

eltham well hall train crash